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HomeMy WebLinkAboutC2006-408 - 9/12/2006 - Approved CHANGE ORDER Department of Engineering Services City of Corpus Christi, Texas CHANGE ORDER NO: ", "- PROJECT NO: 7335 CONTRACT TIME: 180 C.D. Operating Department: Wastewater DATE: September 1, 2006 Name of ProJect: SANITARY SEWER MANHOLE REPLACEMENT OLD BROWNSVILLE ROAD/ OMAHA DRIVE Contractor: BIG STATE EXCAVATION, INC. CHANGE ...!!?Q DEDUCT ADD IbIm A9 24H PVC Sanitary Sewer Gravity Main 55 L.F. @ $500.00 per L.F 27,500.00 IbIm A13 Trench Safety for Excavations 31 L.F. @ $2.00 per L.F 62.00 I~ Al6 Wellpointing 450 L.r. @ $30.00 per L.F 13,500.00 I~ AA2 Trench Safety for Excavations 50 L.F. @ $20.00 per L.F 1,000.00 Item ~7 Removal of Concrete Cradle from under 42" Line 1 Lump Sum 21,548.45 I~ Ale Additional depth of Manhole #9905 1 Lump Sum 24,983.78 I~ ~9 Removal of Grout in 42" line upstream of MH 9901 to install bypass plug 1 Lump Sum 23,978.43 I~ A20 Allowance for Point Repair including all labor, equipment, material, bypass p~ing, traffic control, and pavement repair. 1 Lump Sum 128,000.00 T~ ADD AND DEDUCT TOIIU. NET CHANGE - ADO 240,572.66 240,572.66 Why was this change necessary? If left off the plans and specifications, explain why) of these items was overrun. The to the existing sewer lines at the New I~ Al7 After excavation of Manhole 9905 and the upstream line, a concrete cradle 2006-408 xisting line. This cradle was not shown on any of the plans 09/12/06 M2006-295 Big State Excavation ."~"-- for the exiscng lIne. Remova~~J:_;l~~ line was necessary to replace the damaged FRP ~. New It.. Ala Flowline manholes were taken prior of the lans. Prior to work be innin on this manhole it continued to extra efort to excavate the old manhole and install the new manhole. ---- ..---...-------- New I~ Al9 During the installation of the bypass plug in MH 9901, grout was discovered in the flowline of the pipe. Removal of this grout was necessary in order to properly install the bypass plug so that work could proceed. New It.. A20 During initlal attempts to clean and televise the 27" diameter line segment between MHs 10367 and 10359 (Old Brownsville Road west of Omaha), a significant amount of infiltration and sand was encountered. This is indicative of a large ojening in the line and a potential for a cave-in. Once the location of the source of the infiltration is pinpointed by the televising, a point repair will required. At this point the extent of the repairs is unknown. An allowance is being established for this work. How can These c future? round utilities the exact nature f\~ I' '\ \ f) )Jb~Jc0 the A. CONTlACT PRICE........ ...... ....... $ B. TOTAL CHANGE ORDER (inc. current) .. $ C. NEW ClkJIIbACT PRICE. . .. ............ $ D. THIS CHANGE ORDER........... ....... $ E. PER*T TOTAL CHANGE (B/A) . . .. . .. . . F. PREVIOUS ADDN' L TIME AUTHORIZED... . G. ADDN'L CONTRACT TIME THIS CHANGE ORDER H. TOTAL ADDITIONAL TIME.............. 1,093,730.00 263,153.66 1,356,883.66 .240,572.66 24.06% 5 C.D. 40 C.D. 45 C.D. pp Project Engineer CITY OF CORPUS CHRISTI, TEXAS /: By: ~,4~ ~ ~J~ If ~i ty Engineer :~ /J'i1L LM-/ Title:/~ ~MJ&tet1 . APPROV8~~'~'~~;:~ '~~a~in9 Department j( QP.2/bl. Director of Management , Budget i tAll \i~~tIMlnt c;Ji t:y l.lan6.far ~- City Secretary (y, 2o[,\p- 2- (I) .'OIJ I r1\J "I..~ ----............. ..... /-/ I j If {>>U~C,l__...::Wl.~ ~_ ___.k SEClUM~ /1 t f,- t..--' '~.,'"--.".,...,